Weston wrote on Jul 7
th, 2013 at 4:34am:
It was human error not the airplane that is good
I don't want to sound rude, but lets not jump to conclusions yet. I do lean the same way though. In my honest opinion, there were two issues with that approach, one of them that they either stalled or were just too low, and that they were really right, at least looking at the debris field.
I thought I'd cover some of the things I've heard and my thoughts on them. First off, some news organizations already obtained ATC tapes which are readily available on Youtube, and along with some "experts" have been starting to piece together the series of events. The problem is that clip of ATC on Youtube I've seen CNN use missed a HUGE part of the actual transmissions, where someone assumingly in the background of the tower controlled notices the crash. There are a lot of misleading ideas because of that. What did actually happen according to ATC recordings, the plane crashed, and THEN emergency crews were summoned.
The idea of tired pilots raises another possibility, but that is not the first time that flight has happened, it is quite frequent, along with a flight to LAX under the same flight number, at least according to Flightaware. The idea that the pilots were too tired seems far feteched, especially if I am not mistaken, usually the longest a flight crew can fly in a day is 8 hours (although that is US guidelines if I am not mistaken, and this is not a US airline) which means chances are there was a second flight crew to relieve the first crew. The flight is about 10-11 hours from what I recall looking at.
Now the third and final thing I want to say is that do not rule out mechanical issues. Maintenance among other things could have also played a role. Although it seems there was an issue with pitch and glide slope, there is a chance that something might have lead to that. And they say it was a manual landing, but I do not know where that came from (correct me if I am wrong and missing something). They could have been using ILS for all we know. I think they said that it was a visual approach, but it could have been ILS assisted, and that brought it down.
So it could have been pilot error, just a little too slow and too much pitch, and especially at an airport like San Fran, it can really hurt you. Yet I would wait till we hear about flight data recording stuff, and that won't be long (probably not long till the countless documentaries are made too). It probably is not a repeat of the icing engine performance issue, but it could have been a bird strike that went undetected at the last minute. The only people who know and who will know are the investigators, and the pilot.
Sorry it is a little long, but thought I'd give my thoughts.
-Tom H